Archive for the ‘56040 Reports’ Category

Dereham Workparty Weekend 24th – 25th October 2008

Here is a small report written by my own fair hand, sorry it’s been a while only I’ve been on a foreign holiday…………over to the Isle of Wight (well from Basildon to me it’s a foreign place it’s off the main land).

Any way the attendees/ criminal’s at this little soiree and believe me it was little as well… were the following…. Mickey Doyle, Gareth Broughton, Josh Quirk, and myself the Sheep.

Anyway we were all a bit surprised to see a badly damaged Mark 3 coach that had arrived down on the railway.. But never the less we all surrounded it like a pack/flock of sheep (I felt quite at home!).

So after all the usual comments re the coach, the Grid boys got to work…… not really much to report really. We just carried on where we’d left off the previous week i.e. sanding down, filling, painting and generally trying to tidy her up. As usual it didn’t take long for chaos and pandemonium to ensue. I was brutally antiqued by Messers Doyle and Broughton….. The child claims he tried to warn me, but had a momentary loss of voice!!!!!!!!!!!.

May I take this opportunity to send my very best wishes to Jon and wish him a speedy recovery from his bad back get well soon Jon mate…..

Get well soon also to Keith Wright who has spend the last month in an out of hospital and hopefully is now on the road to recovery.

Well that’s about it for this report (I said it’d be brief), hope to see as many that can make it this coming weekend at Dereham.

Dereham Workparty Weekend 17th – 18th October 2008

A small band of hardy volunteers braved the elements on this particular weekend. Present were Gareth Broughton, Oily Smith, Alan Flockhart, Rod Eastman, Sean Sharples, Josh Quirk, Mick Doyle, Robin Fransham.

Saturday

Oli and Alan got down and started removing the engine room floor panels on ‘B’ side. A lot of sludge has collected under here over the years and it was now very hard for any water to drain away. The sludge was removed and the floor dried off properly and the floor panels taken outside and cleaned. A few more panels need removing to finish off ‘B’ side. Once finished this should really help the damp problem that we’ve had lately. Micky, Child, Sean and Rod had a real blitz on the ‘B’ side bodywork, most of which has now been filled and sanded down. Another good days work and she’ll soon be good for priming. Josh finished off the No 1 end cab side and removed the adhesive that was left behind by the Big T motif. Gareth and Robin made various checks to the batteries.

Saturday evening saw a jolly up to the blue door curry house (eh eh Sharples!), followed by a swift pint in the George courtesy of Sean. Several members promptly tried to debag Sean of his trousers but our attempts were hampered because he wanted to keep them!

Sunday

Alan and Gareth left early for a thing called work (wot’s that then!), leaving Sean, Oli, Mick and Child to carry on with the bodywork. The two gaping holes on ‘B’ side that were patched up with bin liners and No Nails have now been fixed up good and proper with aluminum sheet and copious amounts of filler – this will definitely do as a temporary fix until we can chop the sections out and weld some new steel in. Oli refitted the two cab floor panels and tidied up inside before continuing with the bodywork. Micky and Sean started work on a very tired looking No 2 cab end, which has already started to come up rather nicely!

All in all quite a productive weekend. She’s getting there!

Dereham Workparty Weekend 23rd – 24th August 2008

The day greeted us with rain and whilst the others went for breaky at Morrisons I set to work on removing some more distorted alloy foot plates from the cab steps, the top plate and bolts chiseled off ok, but the second step was a real expletive deleted to get off, in fact it nearly came off in one lump and in the end I resorted to violence and borrowed a jemmy bar to lever it off. I had to leave this job as the rain was starting to get heavy and it was cascading down the side of the loco and it happened to be running right where I needed to chisel and by this time my gloves were soaked through.

Gareth and the get along gang arrived back from breakfast and we duly started the loco, she stared first time and all systems were working ok, the plan was to put 040 on the pit to check the traction motors but Chris Cheney needed to put his green DMU back together on the pit and guess where one half of the DMU was, oh yes down the end of number one siding so a lot of shunting had to be done first and guess who was the only person available to carry out the shunt moves – ME as both Graham and Tim were not in attendance, so myself and Chris
Cheney had a very enjoyable two hour shunt fest to position the relevant vehicles into the right place!

Chris finally positioned 040 on the pit and Gareth went to work checking the traction motors and whilst Gareth did his electrical tests I repositioned a sanding pipe that had in the past been clobbered and the frame had been bent forward and the pipe was scraping a wheel on one of the bogies.

After last weekends last minute find of a sticking fuel pump caused by excess waste oil contaminating the fuel plunger, a full strip down and flush out of the rocker waste drains and associated pipework was required. This was completed by myself and Keith W on the Saturday, a rather dirty job with much sludge being washed out of the drain pipe. All fuel pumps were degreased and re-lubricated with light oil, before a start was made to check that everything was ok, she started fine with just the parking brake interlock valve causing a slight problem, but built pressure and was ready to go!

It was agreed that we would go for a test run to Yaxham after the last train on Sunday, so she was then put to bed for the night.
Sunday morning (or should that be early afternoon by the time we got up!) was spent shunting and getting things in the right order for the evening’s test run, when all shunts were complete she was positioned over the pit so that all traction motor commutators could be visually inspected. Whilst this was going on Keith W went around the inside of Oystermouth making sure all covers were secure and there was no loose items or tools in the engine room that could vibrate loose and cause us problems. All the cantrail grilles were bolted down and the radiator mesh was secured. As usual last minute checks revealed that the fire bottle head which had been shorted out for testing purposes, required further attention before she could be run. This resulted in Robin getting his fingers slightly warm by the melting copper wire he was holding whilst trying to replace the short! She was then fired up, built air and moved away under power up the sidings to allow the steamer to get over the pit, then back up the MOD road to await her first run on the MNR!

With Chris Cheney at the controls we left Dereham at approximately 18:00 heading for Yaxham. At the Dereham level crossings a little banter between a transit horn and ours raised a few smiles – I’m sure you can guess who’s was loudest! After the level crossings she was opened up and away she went – leaving the crossings in a thick clag! Yaxham was reached at about 18:10 and a few photos were taken. Checks were made to the wheel bearings, oil level/pressure, water level, radiator elements, control modules etc, with everything looking good it was decided that a further run would be beneficial. So onwards we went, numerous starts and stops for operational purposes – crossings etc gave plenty of thrash to test the turbos etc, with a noticeable clearing in the exhaust as we progressed – all good signs! The next observation stop was at the level crossing just before Kimberley Park station, where the above checks were performed again which discovered no problems, the obligatory photos were taken and a discussion ensued as to our next move. With spectators on Kimberley Park station awaiting us and the fact that so far so good, it was decided that a full run to Wymondham was in order. Over the crossing we went and paused in Kimberley Park station to await the crossing gates to be closed behind us, this allowed the party that was going on at the station to come and see 56040.

The party was a wedding reception and the children (and the not so young children) were duly invited to have a look in the cabs and sample the horn, creating good PR for the railway and the group. (Is this the first time a wedding has been gatecrashed by a Grid?). After some thank you cake from the party off we set for Wymondham, again reached with no problems, more photos and checks were made before setting off back to Dereham. The return was made similar to the outward journey with regular checks, on approaching privately owned Hardingham Station a figure on the platform was seen, we stopped and was invited for a coffee. After a brief rest we departed again for Dereham were we went into the MOD road, final checks were performed and she was put to bed for the night. All involved went to the pub for a celebratory drink grinning like Cheshire cats!

The test run was successful and no faults were found, the turbos wound up nicely as required, the radiator elements appear not to be leaking, the AWS worked fine, the DSD worked ok, in fact you could say 56040 OYSTERMOUTH is almost back to her wonderful self, just a little more TLC to her makeover and a bit of pampering to go!

Dereham Workparty Weekend 16th – 17th August 2008

Present were: Keith Bulmer, Gareth Broughton, Robin Fransham, Paul Johnson, Oli Smith, Keith Wright, Mark Hallett, Andy Pix, Andy’s Dad David, Graham Miles, Jane Bibey, John Hooson, John Hooson’s son-in-law.

Friday evening

Batteries put on charge ready for the numerous start ups required for testing of systems during the weekend

Sat am

Started her up, but she was missing slightly – the lads down there have got accustomed to this sign of fuel starvation and shut her down immediately. She was manually filled with 500 litres of Diesel ( which was recorded in the repair book). Both fuel rails were bled and a restart made.

Platform side radiator elements – 9 removed and replaced with tested elements from the 20′ container.
We tested some of the removed elements and found them ok (which would indicate the original leak was possibly from the top joint – and running down).

Coach side compressor – removed and dismantled. One of the valves was found to have 2 screws missing, this valve was replaced. In addition it was noticed that some of the pipework was mis-aligned- possibly due to the mix and match nature of the making up of two compressors from 4. The leftover parts from the mix and match exercise were tried and one was found to give a better fit. The compressor was rebuilt and refitted to the loco.

What a difference – the compressor does not knock anymore, and the air builds much quicker than previously, in fact we took the opportunity to test the main safety valve which blew off at a tad over the 11.8 Bar specified- it also closed around 8 Bar which was slightly different from the specified figure but not by much.

Sunday

Started the power unit, but air pressure stopped building at about 3.5 bar- Gareth found the parking brake interlock valve sticking again- this same valve had caused a problem previously and had to be stripped and cleaned out.

The work continued on putting the 9 radiator elements back and the engine was started to test there were no leaks.

At this point a knocking sound was heard and traced to B3 fuel pump, which had stuck in. Investigation with the fuel pump cover off and the engine running showed oil/water being pumped back up the cylinder head drain holes and spraying over the fuel pump. The sticky mess resulted in the fuel pump plunger sticking. The tappet cover was removed and the drain holes were found to be full of gunky oily mess. B4 was removed and water spilled out and a similar oily mess was present.
Mark Hallett was asked to come and give his opinion and the conclusion is the drain pipe needs to be thoroughly cleaned out. Keith Wright and Oli Smith have been shown what to do, and will carry this out next time they are at Dereham. Until this work is done and checked the engine will not be started.

Robin went around the underframe and greased up all the brake rigging, and equalising beams, as well as all the electrical machines (blowers/TM’’s incl Cannon tubes).

During this work Chris Cheney had a look at the tyres and use of the tyre gauge confirmed we have decent profiles on the tyres (which still have turning marks on them showing they were turned shortly prior to withdrawal).

The tab washer on the traction centre needs bending over and brazing in place (I will add to the job sheet).

The two roof hatches on the coach side were opened up with a view to trying to seal them up as a temporary measure. Given the news that Sean is delivering the tarpaulins this Saturday, Gareth and I agreed to leave this work until we can do it properly.
I did, however move and fit missing bodyside filter elements to the louvres nearest the starter motors. A number of filters have been removed and not refitted (including the one in the free end turbo intake ducting – presumably after Carl’s repair – this has been fitted now to ensure we are sucking filtered air into the engine!).

Gareth and I were chuffed (9466!!) with the achievements over the weekend.

Good progress, but it is obvious we need a full set of seals for both the D&M system and the Westinghouse parking brake system. (the PB Interlock valve and one of the brake system governor (pressure switches) gave problems over the weekend).
We have a D&M manual which Gareth and Robin are going to look at . I am trying to find a Westinghouse manual so we can do the same on the PB system.

Very positive weekend but a few warning signs that whilst we have been making good progress there are still a number of components/valves/switches which have only just started to wake up after 8 years out of use- some are waking up nicely and some are a bit groggy and need a bit of attention.

Hope this encourages everyone to the same degree it encouraged me and Gareth.

In addition Andy Pix and his dad David turned up and made a welcome contribution on the radiator element exchanges/testing.
On Sunday John Hooson and his son-in-law Alan came down and dropped of some manuals obtained from the guy who owns 37254. We were about to start her up anyway so it was nice to let John press the button. Gareth showed them around the loco and they went away quite happy.

Dereham Workparty Weekend 8th – 9th August 2008

Another rather damp weekend with Keith Wright, Robin Fransham, Mark Hallet & myself in attendance.

After some rather good detective work by Mark, a special design relay was obtained for the DSD speed switch circuit board. This was repaired first thing and the box remounted on 56040 (but not before it was dropped on my head! – lump available as proof!) An attempt was made to start her, but the batteries were just that little bit too tired to get the speed up, so she was put on charge for the morning whilst work began on removing the axle box covers. The covers were removed to check the condition of the bearings and the grease, the outermost being very awkward as the cab steps had to be removed first! Sounds a fairly easy task, but in reality took several hours to complete – again I was to be found in my usual Saturday position of under the bogies!
These checks revealed no problems with clean soft grease around the bearings with no signs of damage or corrosion. Robin went round with the grease gun and gave each axle a few squeezes of grease, and then went round the break rigging and traction motor blower bearings all lubed up nicely. Investigation into the speedo fault revealed a wiring problem on No.1 end cab, there are two positives and two negatives in the wiring loom behind the desk for the speedo’s, a pair of each for the main speedo and another pair for the slow speed speedo, somehow both positives were wired on the slow speed speedo, whilst both negatives were wired on the main speedo! This was rectified and everything was ready for testing.

Oystermouth burst into life, but after a few minutes the air was not building as expected, a rather large gushing noise was heard coming from the parking brake frame. Upon investigation it was found that the parking brake interlock valve had stuck, the engine was shutdown and air isolated from the parking brake. The valve was stripped down to reveal that it was full of that wonderful substance that gets everywhere – water! The valve was removed from the loco, stripped, freed and lubricated before being rebuilt and replaced on the frame. Time to press the button again with fingers crossed! This time she fired up and was building fine, checks revealed that whilst removing the interlock valve, we had accidentally damaged one of the pipes leading to the valve – one of the problems associated with fixed pipework which has to be strained to release valves etc. This was patched for testing purposes with a solution Heath Robinson would have been proud of! Air then built up nicely and she took power straight away with no problems!

The DSD time was allowed to elapse and this dumped the main air pipe confirming that the newly repaired DSD box/relay was working, after 2 minutes time delay the pipe was returned and power could be obtained again. A quick trundle up the siding proved that the main speedos in both cabs were working, and on the return the slow speed control was switched in proving the slow speed speedo’s were working – and that the traction control module worked well as she was increasing/decreasing power in order to keep a steady speed. We shut her down for the night, removed the temporary repaired pipe and another pipe from the unloader valves so that replacements can be manufactured. All in all a rather wet but successful day!

Dereham Workparty Weekend 26th – 27th July 2008

A very hot day at Dereham, Gareth Broughton/Jon Batley/Robin Fransham and Keith Wright were in attendance.
Work achieved :-We fired her up and she built air straight away, held it and took power – as good as gold!
We shut her down to work on a few air leaks on the No1 desk which were cured by removing a panel and tightening up a loosened union, and we looked into a fault on the AWS which involved us spending a few hours under No1. bogie.

We rubbed a magnet under the AWS dome with no success so the next thing was to remove the AWS dome, after finding the correct size socket in Jon’s tool box, we undid the dome, but due to the lack of space under No1 bogie, and indeed the 26 degree heat it was a slow process. Once all the bolts were undone, the dome still would not budge, it seemed there was rivet of some sort holding up proceedings so we borrowed a small bladed screwdriver off Keith Wright to see if we could prize the dome off but Jon duly broke it (sorry Keith!) so Jon resorted to drilling out the offending rivet with a cordless drill – cue hot shards of metal down Jon’s boiler suit and copious amounts of laughter form Gareth and Robin, couple that with Gareths passing of wind made it a great place to work!

Once the dome was succesfully removed Gareth went to work with his electronic trickery to see if there was a fault within, all we could hear was a ‘clicking’ as the magnet passed across, whilst Gareth/Jon and Robin were having their party under No 1 bogie, Keith W went to work on No 2 cab re-assembling the dials/switches (the right way round this time, ahem!).

Keith also cleaned up the sun visors in No 1 cab, by removing them and giving them a deep clean!

We left the AWS fault and fired her up again and she built air again, slightly slower this time, but again held it ok and took power. Shut down again and worked on some more faults etc, then started her again, this time she built as expected and took power. Now we think that it is possibly little bits of corroded pipes etc floating about in the system and intermittently sticking non-return valves or some of the EP valves on the parking frame, thus causing the pressure not to build.
When we did the tests we bled all the air out using the valves on the tanks next to the compressors and there was quite a bit of damp and bits coming out, we think this should eventually settle down – just a matter of working everything through the system. On the last attempt we loaded up the reservoirs and then opened up the isolation cock allowing 6 bar to blast through the system rather than build up all the system slowly, this had the effect of blowing her nose and dislodged a few bits and bobs.

The DSD speed switch unit was removed for repair.

Dereham Workparty Weekend 24th – 26th May 2008

Attendees for this work party were as follows:
Sean Sharples, Graham Miles, Josh Quirk, Keith Wright, Andrew Wilson, Gareth Broughton, Mark Lynton, Sue Jarvis, Jane Bibey, Chris Cheney, Robin Fransham, Mickey Doyle, Alan Flockhart, Mark Hallett, Oli Smith

I only attended on Saturday 24th May and this report covers that day. We started work about 09.45 on 56040, we all knew roughly what we were supposed to be doing and simply got on with our tasks (which is great!) as we don’t need to be constantly told what to do and how to do it. It was good to see Brillo up and Mark and Sue again, congrats on getting your Mid Norfolk P.T.S certificates also it was good to have Mick back from his soiree with the Red Arrow’s in Cyprus.
Garlic and myself set about changing a starter motor (God those things weigh a ton!) first carting the knackered one out and then getting the good one in and believe me this was no easy task, well done Garlic!!!!,
It was good to see the new compressor joint go in that the maintenance boys have made for me at my works.

Well done Robin and Keith the cab for fitting it – job done.
Good to see Alan man up the sharp end up to his armpits in grease getting stuck in. Thanks also to Chris for loaning Garlic and myself his socket set to enable us to change the starter motor – thanks very much Chris you are a star!
It was great to see “Keith the cab” back, no pun intended mate, after his op and getting stuck in. We tried to start 56040 up after the new starter motor was fitted and she duly obliged – superb!!!!!
After being shut down we thought we would give the Teddy Bear punters a treat and fire her up again, but would you believe it she just doesn’t seem to like an audience and she just wouldn’t start.
After a few slight technical adjustments she duly obliged.

Josh, Mark and Graham carried on with the painting of the bogies and bodywork and the quality of the painting is phenomenal. Josh also helped out in the engine room.
Whilst this was going on members of the work party were busy putting the rocker covers back on.

Jane as usual fed us, thanks mum again, you’re a real star considering your on board catering commitments to the Teddy Bear specials you still managed to squeeze in time to feed us.
Well after getting quite a lot of work done on the old girl we discovered some circuits that needed some attention they had been inoperable for some 8 years and needed some looking at. Hopefully we can make some headway in that department this coming weekend, as we now have a group of top notch techno boys on the case – you know who you are so enougth said!
I noticed I was getting a few comments when taking all the photos of what was happening, remember if it’s not recorded it’ll be forgotten and we need to keep an accurate record not only for ourselves but for other members of the Grid group who for whatever reason cannot make it to Dereham, to keep them up to speed with ” Oystermouths ” progress. Don’t forget also that we are volunteers not paid staff!

Dereham Workparty Weekend 26th – 27th April 2008

This working party was a lot smaller than usual, due to the working party having to be split over two weekends (this weekend and the next), due to problems with availability of personnel. Keith Wright dropped in on Saturday morning and did a bit more work on the No 1 cab, before going off to work at a model railway exhibition, while Graham Miles worked on rubbing down No 2 cab over the weekend. Jon Batley spent the weekend working on the loco steps, and was joined on Sunday by Sean Sharples who did a bit more bogie work, and Oli Smith who worked on the No 1 cab nose end, removing the horn grill for de-rusting.

Back up at the Sleeping Coach, our younger member Josh Quirk helped Jane Bibey with the toilet and drain cleaning, and cooking the members meals (before Jane hits me, please note that this wasn’t done at the same time ! !). Jane also learned the hard way, that she needs to check that Josh has wound his watch up, before asking him to take the fudge brownies out of the oven at a certain time. Chocolate Fudge Charcoal anyone ????

While all this was going on, I drew the short straw again, and was exiled to the “Black Hole of Calcutta” that masquerades as the inside of “Oystermouth”, to start the repairs on the blown air pipe under the walkway in the electrical cubicle. One of the air pipes that passes through the underside floor plate had rusted through at the union which passes through the plate, which had then burst during an initial test of the air system. The original plan of action was to disconnect the air pipe underneath the loco by the bogie, disconnect the air pipe inside the electrical cubicle, and cut out the damage union out using a 2″ Starrett cutter.

That was the plan, but events turned out a little different. An earlier attempt to start this work had foundered, due to not having a 30mm crowfoot spanner to undo the air pipes underneath and inside the loco. Now equipped with this crucial (and expensive) tool, this part of the job was completed relatively easily, and the underside pipe was sealed up to stop dirt falling into it and causing problems later on. The next stage was to cut out the the damaged union.

It was at this stage that we hit a few problems. The first problem was that a second union was found to have a fracture, which would burst in time, so this would have to be dealt with at the same time. With the air pipes to this second union disconnected and sealed up as well, cutting could start. This is where the second problem came to light, namely that the underside floor plate while not that thick, was a tough as old boots. I’m not 100% sure it was mild steel, more like armour plate. By the end of cutting, the 2″ Starrett cutter was totally blunted and burnt out. And it was also borrowed from another group on the MNR, and will need replacing ! !

The third problem was that very near to where I was cutting, the floor appeared to be alright, but the heavy vibrations from the cutting soon shook the rust out, leaving a few small holes, near to the other air pipe unions. This might mean we have to do more dismantling and cutting later on, and then re-plate a larger area. This could be real fun in such a confined space.

The next thing we need to do, is get two new new bulkhead unions manufactured, which is now in hand. Once these are back with us, we have to decide what to do with the underside floor plate, regards cutting out the rest of the rust, and then re-assemble everything. Another b###s ache of a job lies ahead.

Dereham Workparty Weekend 29th – 30th March 2008

The working party over the weekend of Saturday 29th and Sunday 30th March went very well, and although we had a smaller turnout than previous working parties, a lot of work was still carried out. Graham Miles, Sean Sharples, Jon Batley, Oli Smith, Josh Quirk and Jim Knowles carried on the task of cleaning and painting the bogies and brake air pipes. Their work is starting to have some marked visible results, with one half of one side of “Oystermouth” from the mainframe down, now being totally renovated.

Keith Wright carried on with the renovation of the No 1 cab on “Oystermouth”, although he did cause some major worrying, when I noticed that he had painted the cab desk in a bright shade of pink ! ! I was trying not to look or sound ungrateful after all of Keith’s hard work . . . . but pink ?? Luckily it turned out this was only the undercoat, and the finishing topcoat would be grey. What had made made me think that this was the finished product, was that all the cab gauges and switches were all screwed back in. What I hadn’t realised, as I hadn’t been able to get to Dereham for the middle weekend in March, was that this was done for the MNR Diesel Gala, where “Oystermouth” was on display in the bay platform. It might have had an effect on the number of people volunteering to drive “Oystermouth”, had the finished interior been pink ! ! A big butch Grid with a pink interior . . . . oh my gawd ! !

Carl Rayner fabricated a new angled plate, to patch the hole in the air inlet on one side. While Carl did a very good job of this repair, the metalwork forming the surrounding area is showing signs of corrosion, and this will mean that in a couple of years time, we will have to carry out more repairs to this area. The roof is actually the biggest area of “Oystermouth” in need of major anti-corrosion work, with a lot of rust present at cantrail height and with holes further up at the top, as evident by the water leaks when it rains. Luckily this doesn’t stop us getting “Oystermouth” started up and hauling trains, but eventually we will have no choice but to remove the roof and carry out some major anti-corrosion repairs in a couple of years time ??).

On the Saturday, David Woodhouse came over with his JCB and forklift attachment, and helped Micky Doyle and myself to fit the second compressor to “Oystermouth”. This is the last large item to be re-fitted to “Oystermouth”, and marks a major event for the Class 56 Group, as for the first time in our ownership and for the first time in many years, “Oystermouth” is a fully complete locomotive (bar a few switches, etc). Micky and myself then tightened the four mounting bolts on this compressors, and the four mounting bolts on the other compressor, that was fitted to “Oystermouth” during the February working party.

Over the rest of the weekend, I refitted all the air pipes and hoses to both compressors (sealing them all with PTFE tape), including one that we thought we didn’t have, but luckily Carl found hidden in our spares container. When I refitted the expansion tank to the second compressor, its mounting holes were offset and in a different position to the first compressor. This meant that with nothing to base the re-assembly on, I had to make a guess as to which way round it all went. Luckily I got it right first time, which was nice, as having to drop the compressor back down to turn the expansion tank and cradle around would have been a real pain ! ! The only thing to complete on the air pipe side of things, is to tighten both loco to expansion tank pipe connections. Unfortunately it’s impossible to get a spanner or adjustable spanner onto this. The only thing that will do this job is a 48mm crowfoot spanner, which will cost about £40 to £50 and would have to be a special order. An alterative might be to see if I can get one made. I assume that BE / EWS had a special tool for this job ! !

I also refitted the electrical conduits to both compressors, but I left the connecting of the magical “blue smoke” wires to our resident expert Gareth. Unfortunately, if the wires are connected up wrongly, the compressor will run in reverse, which will damage it. Not what we want, after all the hard work we’ve done. I connected the earth lead on one compressor, but the second one had it’s mounting post missing, so I’ve left that for Gareth as well.

Once this was all done, I drained the old oil from both of the compressors, and filled them with the new compressor oil we had in the container. Once this was done, Josh cleaned the underside of both compressors and then finished painting the undersides black, which we couldn’t do when they were sitting on their pallets in the goods shed.

A big thank you to Jane as well, for the excellent food that kept the lads fuelled over the weekend.

Dereham Workparty Weekend 23rd – 24th February 2008

COMPRESSORS
1st compressor fitted (to station side) needs jacking up and bolts fully tightened, but all 4 bolts are fully engaged in the nuts so it is safe to move the loco.
The air and electrical connections need remaking.

2nd compressor has been rebuilt with parts obtained from Metcalfe. Thanks to Alan and Mickey who worked late on Saturday evening (Alan worked until10pm I believe).

The fact we have never seen 040 with a compressor underslung meant she looked a bit strange for a while but this has to be the major achievement of the restoration so far. Well done everyone!

OIL
Hallett oil delivery arrived at 9-15AM.

To my surprise the SF47G did change the oil in 47 596, so we used the oil from 596 to fill 040 for flushing & initial system testing.

This took longer than we thought as reducing the flexible pipes down using Jubilee clips proved less than easy. At one point there was so much oil flying about we considered chucking the Oystermouth nameplates and getting some Torrey Canyon or Amoco Cadiz ones made up!

Eventually we used the bulk filler connection- and Mark Hallett’s big pump and got oil into the sump- it settled at about an inch below the standing max mark on the dipstick.

The Hydrostatic tank was filled up and then the two oil filters elements were replaced.
The crank case doors were removed ready for oil priming tests and the lube oil pipes were removed to allow access to the cam trays which have been refitted.

Unfortunately the priming test did not proceed due to one of the local push buttons in the engine room being full of water. However we do know the priming pump runs as the other push button had jammed in and the pump ran as soon as the circuit breaker was in.

The first signs of life from the old girl were the priming pump running (for about 10 seconds) and then the fire bells ringing!

The waterlogged switch will be repaired /replaced and Gareth is going to make up some dummy sensors for the fire bottle system.

BATTERIES
A couple of defective cells were exchanged with some of the ones Edward brought over- surprisingly the common view on these cells is that they are all in rather good condition.

BODY, BOGIES AND CABS
Work continued – the bogies are starting to look really good now, and the No 1 cab is going to look superb. Keith Wright (or Keith the Cab as he is now known) is doing a really good job. He has undercoated the drivers desk and all the instruments have been removed .(In fact I had a Booths flash back when I saw the gaping holes where the speedo etc have been removed)

EXTRA DETAILS ON BOGIES/CAB (NO 1 END) by Jon Batley

Graham Miles, Jon Batley, Oli Smith and Sean Sharples concentrated on the the bogies at No 1 cab end, Jon finished scraping off the old paint on the cab kickplate, it’s now nice and shiny! Sean and Oli did a great job painting the bogie and associated pipes, Graham continued painting the brake/main res pipe cocks and connectors. On Sunday Jon started removing the paint from the multi-working socket and painted it in primer ready for repainting, Oli Smith went under the loco in the pit and got filthy cleaning the underside of the sanding boxes and the buffer beam.

FUEL SYSTEM
Coarse fuel filter filled with clean diesel and lid refitted (missing studs replaced from ex-56044 filter housing – thanks to 56044 and Alan Flockhart.

COOLANT SYSTEM
The coolant system was filled in anticipation of turning her over on the starters but we didn’t get that far so we drained her down as a frost protection measure.

NIGHT TIME SHENANIGANS (report by Jon Batley)
Eight of us Keith B, Keith W, Sean, Gareth, Josh, Alan, Jon and Oli hit the town for a well deserved curry after a hard days work, the Indian was fully booked so young Josh took us all to a Thai Restaurant. A great time was had by all and its events like this which makes the weekend so good, I don’t think that I’ve laughed so much in ages, it was my first time out with the group for a weekend and it was great to get to know the guys on a personal level, not only are they great to work with but the social side of the group is second to none, and I urge any prospective Class 56 members/volunteers to come and sample a weekend/ night out with the team.

After the meal we went to a local pub and chilled out with a pint (or two or three….). A perfect end to a great night out, thanks lads I will be back next month for another night out!!

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