Posts Tagged ‘mnr’

56101 – Cooler Group repair progress

9th – 11th July

Friday we were blessed with good weather and for the weekend ahead this meant that we could progress a little closer towards the removal of the cooler group. Oli and myself set to and made a start on removal of pipework, access panels etc. What we didn’t expect was how hot it got during the afternoon 29 degrees outside, 34 degrees inside! It wasn’t long before trips to the tap ensued and all to quench our thirst and replenish the fluids which we sweated out. I managed to remove all the bolts that secure the intake duct to the No1 end turbo and move it out the way for access, that was enough for the day.

Saturday was pretty much the same this time, working alone I set to and made a move to remove the main water pipe that connects to the top water rail, this was the more awkward of the pipes to move clear. This also took most of the day to do purely down to the shear heat of the day as Saturday was a scorcher too!

To cap it all off I think that we are nearly in a position to remove the remains of the cooler group and crack on with the repair. As always, any extra man power at this stage will be greatly received, even if you can only spare a few hours. Please get in contact with the group using the button on the right.

More to follow…… Mick Doyle

56101 Work Report, 3rd July

It all started on Friday afternoon shunting the stock out of the way in order to release 56101 that was stuck right down number 1 road at Dereham. Myself, Oli, and Josh managed to complete the shunt in two moves and leave the 56 on number 2 road ready for Saturday morning.

On Saturday morning Myself and Josh set to on the removal of the remaining grill and roof panel, as to be expected we did shear more bolts in order to get them off but never the less they were removed without any incident. Armed with a tin of “Gas Oil” I sprayed all of the studs and let them soak, Josh was removing the three access panels that located inside the cooler group tunnel and I made a start on the removal of the first batch of elements. With only 7 out of the 10 elements remaining I managed to shear more of the studs, bearing in mind that the elements are made primarily of copper and the main objective of the exercise was to remove the risk of theft, either way they had to come out and be stored.

Because the loco was positioned in the MoD platform we were in the way, and stock stored in the main platform meant that we had to shunt release the service train when it returned. I was using the ONLY serviceable loco at the time at Dereham, 50 019 “Ramillies”, to shunt the 56 out of the way and perform the shunt release and pick the 56 back up to continue the work, so as you may gather we were a little bit busy during the day. Never the less we managed to complete the task and remove, store and clean out the cooler bay with 5 shunt releases thrown in.

Please do not be fooled into thinking that there can’t be much work for us to do, on the contrary! It is a big job and we need all the hands we get so we can overhaul the cooler groups in turn. If you can spare a day or two, please get in touch with the group via the group email address – class56group@hotmail.com

Mick Doyle

All of the radiator elements removedEmpty radiator bays on 56101 – note the rear cooler group tunnel covers removed.

almost thereNearly there – 2 of the 3 radiator bays have been emptied of their copper radiator elements.

Years of coal and grime30 years of hauling MGR trains has taken it’s toll!!

56101 Update

Firstly, a huge apology to those who turned out on Sunday expecting 56101. While we managed to get word out on some of the forums that 101 would not be out, this website was not updated in time with the bad news. The following report is from Mick Doyle.

For all those out there that had the wasted journey I am sorry. There is an issue with 56101 being water tight and this has worsened since the Thunder-bird run to rescue 20069 after she failed at Wymondham 2 weeks ago. Gareth Broughton was duly informed on the severity of the leak and that it would need to be rectified at the earliest opportunity – this meant that the loco was still under repair and wasn’t officially declared SERVICEABLE.

Gareth started the strip down but with no surprise sheared one of the lower studs that secure the radiator element to the lower water rail, because of the lack of time the job was left to me to see if I could do anything to try to rectify the situation. The answer to that would be NO! I managed to shear another two studs – oh hell! So this means that after a lengthy conversation yesterday with Gareth we agreed that the cooler groups will come out for repair and the voids will be cleaned and painted. To this end 56 101 will be out of service for the foreseeable future.

Once again appologies to those who made a waste journey.

Bottom manifold sheared bolts The sheared studs on the bottom water rail of one of 56101’s cooler groups.  Photo: Mick Doyle.

56101 running day – 20th June

As promised! 56101 will be out at the MNR, Dereham, on Sunday 20th June. The loco will be working the Orange timetable with the line’s Blue/Grey Mk2s. It’s planned for 56101 work all three round trips: 1015, 1300, 1515 from Dereham and 1115, 1400, 1615 from Wymondham – just over 66 miles in all.

Fares and details on how to get to Dereham / Wymondham can be found at http://www.mnr.org.uk. Please note that while every effort is made to provide the advertised traction, the railway and loco owners reserve the right to change this at short notice.

Swanage Diesel Gala 2010 028 56101 at Swanage during the Diesel Gala on May 9th. Photo courtesy Mick Doyle.

Mutual Improvement arrives in Norfolk

As reported earlier on last week, 56101 has now safely arrived in Norfolk. GBRF arrived on the MNR branch with the loco around 1600, slightly earlier than planned. Some photos below taken by our very own roving paparazzi Geoff Tibble show the ‘Grid’s arrival in the flatlands! The idea of a running day with 56101 in the near future is being discussed with the operations team at MNR – rest assured you’ll read about it here first!

DSCF2089
0A56 arrives at Wymondham Junction

DSCF2108
56101 is fired up on MNR metals

DSCF2141‘101 put to bed at Dereham

56101 on the move!

Privately owned 56101 will be on the move to the Mid Norfolk Railway tomorrow, 26th May. Grid ‘101 will be taking up duties at the MNR’s Dereham base for the forseeable future while group loco 56040 is off site for repairs. GB Railfreight will be moving the loco working as the 0920 0A56 service from Eastleigh Works – Dereham MNR, hopefully arriving shortly before 1700.

Some rough times are thus: Eastleigh (09/29), Basingstoke (10/04), Woking (10/30), Hounslow (11/24), Willesden Jn High Level (1141 – 1143), Upper Holloway (12/01), South Tottenham Signal 1004 (1214 – 1225),  Stratford (12/47), Cheshunt (13/22), Harlow Town (1333 – 1339), Stansted Goods Loop (1356 – 1419), Cambridge (1443 – 1446), Ely (15/01), Brandon Down Goods Loop (1525 – 1555), Wymondham (1622 – 1626), Dereham (1646).

Photos greatly received!

56101 Swanage box 56101 at the recent Swanage diesel gala on the 9th May. Photo courtesy Mr Rodgers Snr.

56040 to visit Battlefield Line for repairs

After investigating a number of options with regards to the work required to replace No. 1 & 2 traction motors on 56040, an opportunity has arisen which allowed the work to be undertaken at reasonable cost providing 56040 was made available to appear at the Battlefield Line’s upcoming Diesel Gala on 18th to 20th September.

The repairs to Oystermouth, which will be completed after the gala, will see work on 56040 carried out alongside Edward Stevenson’s 56098. The combination of the work on both locos was critical in reducing the cost of the crane hire necessary to do this work safely and efficiently.

It is likely that 56040 will depart Dereham between the 17th August and the 17th September - anyone wanting to see the loco before it leaves or indeed during the journey should keep an eye on this website.

Regards,
Class 56 Group Committee

56040’s passenger debut

Well what can I say! A fantastic weekend was enjoyed by everyone who attended this gala. 56040 performed perfectly with no faults reported even though it had two traction motors isolated. The mechanical, electrical and paint team pulled out all the stops to get 56040 fettled for the gala and work continued well into the night in the week leading up to the gala. Congratulations and many, many thanks to them for their sterling efforts and also to anyone who has assisted in any way on the restoration of 56040. The paintwork looked absolutely stunning and I had to take a step back when I first saw it on the Friday morning. I was there for the full three days to enjoy the festivities and must say that it was one of the best diesel galas that I have ever attended and not just because 56040 had a starring role! I spoke to many people over the weekend and the only criticism that I heard was that it was just too packed on the Saturday. Timekeeping was exemplary and credit for this is due to the drivers, yard staff and shunters who coupled, run round and uncoupled locomotives with the minimum of delay. Grateful thanks also to the MNR staff who were as conscientious and professional as ever throughout the gala. All the locomotives performed well with everything working its booked diagram with no failures. The only slight difficulty was that 66144 and 67008 wouldn’t multi but to alleviate this two driving crews drove the engines in tandem.

Friday

I missed the first departure owing to late arrival but when I did arrive it was good to see punters queuing out of the MNR booking office door at Dereham even though it was a Friday. The day rover fare was very reasonable considering what the punters were getting for their money and this probably contributed to their presence en masse. Some preserved railways charge unrealistic day rover fares, especially in the current economic climate, and they then wonder why most of their trains run almost empty! The weather was not too bad considering that it was still March, cloud with the odd burst of sun and a brief shower every now and then. At 10.00 37425 and 73210 arrived back at Dereham with the first train which were then removed. 56040 then burst into life driven by Mickey Doyle with Gareth and Keith in the back cab to diagnose any faults during the runs and the clatter of hundreds of camera shutters could be heard as far away as Norwich. 56040 then backed on and I was told that there were no faults reported after the previous night’s loaded test run, even though two traction motors had been isolated, and that it was all systems go. 56040 then got the whistle and thrashed out of Dereham. 56040 was a scratch for me, and many other people I spoke to, as it had only worked one railtour back in 1995 although it had worked on drags before this. After what seemed like only a few minutes we arrived at Wymondham. The train then continued to the loop for 56040 to run round and most punters stayed on to squeeze in those extra few chains of mileage. I got off for some historic photographs of 56040 on its first public train in preservation. The train returned to the platform having run round and I got back on. It was pleasing to see that nearly every seat was occupied. The stock was air-braked, load six with two first class vehicles in the consist giving a passenger loading of just over two hundred. Some of the gala attendees asked why more coaches couldn’t be added to the consist but the answer is that the MNR only has six air braked coaches and six vacuum braked engines and are obviously not interchangeable. The next train had 60059 drop onto the front with 56040 on the rear. 60059 hauled this train to Wymondham with 56040 dead at the rear. At Wymondham 56040 fired into life again to take us back to Dereham. The Class 56 Group sales stand was in attendance in the brake coach all three days, manned by Paul, Alan, Oily and Mark and business was reported as brisk. The 14.00 departure had 67008 and 66144 on the front with 56040 again dead at the rear to Wymondham. At Wymondham 56040 was then leading for another run back to Dereham. 56040 was then removed from the train and after a game of shunt musical chairs it was attached to the front while 37425 and 73210 were coupled up and attached to the back. The final train of the day, the 16.00, was hauled by 56040 with 37425 and 73210 dead at the rear. The sun had reappeared by this time but it was extremely difficult to get a clear shot of any locomotive due to the amount of people that were on the platform getting in the way. The final run of the day was the 16.45 from Wymondham which had 37425 and 73210 leading with 56040 at the rear. Back at Dereham more shots were taken of 56040 by a very happy gala contingent and 56040 was retired for a well earned rest for the night. The volunteers, after a hose down and degreasing, went into town for a much needed meal and a drink (or two or three!!).

Saturday

I missed the first departure AGAIN, this time due to an extra round of toast placed in front of me at breakfast (well, it wouldn’t have been polite to refuse would it)? I had missed the 8.15 departure which had 37425 leading and 20069 and 73210 at the rear. The punters were queuing out of the door again and the car park was full at 8.30. I took a few photographs and waited patiently for the return of the 8.15. The platform had started to fill up and I knew that the trains were going to be extremely busy. I decided to just photograph that day and help out the Class 56 Group if needed as I hate travelling on crush load condition trains. The weather had deteriorated badly overnight and now was driving rain with a bitter, freezing cold wind blowing. This didn’t deter the crowds however and when the 8.15 returned everyone dived on for a seat. The 9.50 was booked to be hauled by 37425 again with 50019 on the rear. 50019 had just returned to traffic from a long term overhaul and some people wanted a blast behind this. The train duly departed and it was full and standing as predicted. I took some photographs in the rain, went for a cup of tea and waited for the return of the 9.50. This is were the fun started. 60059 buffered up to the front of the train and 56040 was attached to the rear. Most people on the incoming train wisely decided to keep their seats when they saw the crowded platforms. When everyone had boarded the train there wasn’t a space to be had anywhere. The platform staff at Dereham even had to push people into the trains Japanese style it was that bad! At 11.45 the whistle blew and 60059 departed. At Wymondham 56040 was now leading to Dereham. This formed the 12.40 back to Dereham. People were being turned away at Wymondham booking office because they couldn’t physically get them on the train. A passenger count on the 12.40 was heroically conducted by the guard (I don’t know how he managed this!) who reported that there were over 500 people on a 218 capacity train. Back at Dereham legs, arms and heads were carefully untangled and people fell out onto the platform in a steaming heap. The 13.45 departure from Dereham was just as bad loading wise with 56040 and the DBS engines 67008 and 66144 on the rear. I was glad that I had plenty of space on the platform even though it was freezing cold. More photos and another cup of tea passed away the next hour until the 14.40 from Wymondham returned with 67008 and 66144 leading and 56040 dead at the rear. Things quietened down a little after this and 37425 took out the 15.45 from Dereham with 31438 at the rear. When the train left I noticed Jane and Paul had been left behind. They said that they had run out of beer and there was nothing left for the beerex (Hmm, a beerex with no beer – that should please the punters)! A mad dash by car to a local brewery to collect five more polypins and two boxes of bottled beer was thankfully successful and I helped them carry the beer from the car to the platform. 31438 then brought in the 16.30 from Wymondham with 37425 on the back. A big shunt around then ensued with 60059, 67008 and 66144 going on to the front of the train with 56040 at the rear. Many punters had stayed just for the beerex and mega haulage so cries of ‘teas, coffees, light refreshments but no beer’ wouldn’t have gone down very well! Finally 56040 returned from Wymondham at 19.05 hauling six coaches and three dead engines. It handled this task spectacularly and no problems with 56040 were reported. 56040 was put to bed again ready for Sunday’s happenings.

Sunday

What a contrast to Saturday. The day was bright, sunny and quite warm. There weren’t as many people at Dereham as there was on Saturday but it was a good Sunday attendance nevertheless for a diesel gala. I decided to forego the extra round of toast for the benefit of my figure! this time and arrived in time to view the first train which was the 9.00 from Dereham with 50019 in charge and 60059 trailing on the back. I was planning to do another day rover but got talking to some punters on the platform and let the train go instead. When it returned at 10.25 with 60059 leading I took some further photographs and was then asked if I would give a hand with some yard tours along with other volunteers as I held a PTS for the MNR. This was a great idea by Jon Batley and I was happy to help, the yard tour took place after the 10.50 train had departed with 37425 leading and 56040 on the rear and Jon had checked over the radio that there were no shunting movements planned. The visitors were allowed, within reason and at all times under our supervision, to access the top yard for number taking and photographs. This was a huge success and the punters were extremely grateful to be offered the chance to access the yard. Many of them remarked on the way back how different this gala had been from other galas elsewhere with loco sheds and yards totally out of bounds, expensive tickets, crappy coaching stock and miserable staff. We got all the yard visitors back within the boundary and awaited the arrival of the 12.20 hauled by 56040. We heard it long before we saw and it made a fantastic sight coming round the corner in full sunlight with six blue/grey Mark twos behind it. 56040 was then removed for a rest and a drink of water whilst 60059 went on the back and 66144 and 67008 went on the front of the 12.45 departure to Wymondham. Time now for a visit to the buffet for a cup of tea and a gossip. I went back on the platform and awaited the arrival of the 13.40 from Wymondham which was due in Dereham at 14.15 hauled by 60059. When this arrived another big shunt was done to get 60059 round to the front of the train to be joined by 20069 and 37425 to the back of the train. This departed at 14.45 and after this had left Jon called us all together again to steward the final visitor yard tour of the day which again was appreciated by everyone taking part. The final train of the gala was hauled by 37425 according to the timetable with 56040 on the rear. What actually happened was that 37425, 60059, 67008 and 66144 were coupled to the front of the train so that the DBS locos could run directly back onto NR metals when uncoupled at Wymondham. This departed at 16.45 with much tooting of horns and after this I took my final photographs in the yard in the early evening sunshine, said my final goodbyes and then left what had been a most memorable gala and most enjoyable long weekend.

A full photo gallery has been added here, but here’s a taster below;

26-03-09DJ1

56040 starts for the first time since storage by EWS

A momentous event in history occurred on 4th May 2008 at approximately 21.00 when 56040’s engine was started for the first time. There had been a workparty on this particular weekend however most people had gone home by 21.00 and there were only a few people remaining to observe the spectacle. The engine was idling for a few minutes and a couple of minor problems were encountered. These have now been resolved. A message of thanks from the Class 56 Group Committee and Directors of Class 56 Locomotives Limited follows:

Congratulations are due to EVERYONE who has ever worked with or for the Class 56 Group or on “Oystermouth” . This really is a team effort that goes back over the last sixteen years, right to the very early days of the Class 56 Group. While the people working on “Oystermouth” today are of course due special thanks for their hard and often dirty work, let us not forget the other hard work carried out by a vast multitude of other people over these sixteen years, even if these people aren’t here today. Every single bit of work, carried out by every single one of these people, has bought us to this momentous moment of not only purchasing a Class 56, but getting it running again. Everyone has done, or still does whatever they can do to help out, and just because someone is or isn’t at Dereham every weekend, this doesn’t diminish in anyway any of this hard work. Even the ordinary Group member paying their annual subscriptions has done his or her small part

Remember . . . .with even the smallest cog missing, the biggest machine won’t work. No one is better than the next person in this team ! !

THANK YOU TO EVERYONE INVOLVED IN “TEAM CLASS 56 GROUP” OVER THE LAST SIXTEEN YEARS . . . . enough said.

Alan Hawkins

Dereham Workparty Weekend 15th – 16th November 2008

The usual suspects turned up with a few bit part players from time to time. Good to see Keith Wright return to the fold. Anyway, Saturday began with us topping up the anti-freeze that’d been delivered during the week, and then the water was topped up also.
We went for a start up around 1600/1630 hrs but as usual Oystermouth never fails to disappoint and would she start, would she heck.
The call went out ’send for Gareth/Garlic’ and no sooner had he and his trusty screwdriver arrived then he’d sussed and sorted the fault out, apparently it was the LPC (Lub Prim Contact D), which apparently wasn’t making the start up circuit complete.

Repairs were duly carried out with Gareth plying his trade in the electrical cabinet and myself holding the wiring diagram and torch for him, 56040 duly obliged and started up.

Oh, I must just mention the ‘unusual’ clock (I said clock!) that Mickey Doyle had, a most unusual ring tone as the boys found out when someone set the alarm to go off during the early hours of Sunday morning. I don’t know which was funnier the alarm going off or Chris threatening to do all manner of things to Josh, who he wrongly thought had set the alarm.

Anyway now to Saturday Night.

It was off to the King’s Head, North Elmham for the usual blow out with a little bit of p*ss taking thrown in for good measure.
Three car loads set off from Dereham around 1915/1930 hrs, and duly arrived at the said watering hole. A quick chat with the Landlord and we were shown to a table. Seated were the following, Gareth and his significant other Ada aka Laura (Happy Birthday Garlic), Mickey and Clare Doyle, Mark Hallet, Chris Chaney, Robin Fransham, Keith Wright (Or to use his proper name Keith the cab), myself the sheep (oh by the way lads thanks for the little pressie baa baa baa , the other half loved it), Josh the child and finally but not lastly Mr James Steward in person. Anyway the alcohol flowed and the grub arrived, oh how I wish I hadn’t had the mixed grill (if you’d had it you’d know what I mean). Cue the chaos and mayhem, we decided to tone it down a bit as Garlic’s other half obviously wouldn’t be used to it. When I asked Gareth what Laura had made of the night? He said she was slightly surprised how tame we all were, anyhow much to my surprise, Mick and the rest of the boys had ordered dessert. When his trifle arrived he offered me a ‘spoonful’, (no not a 47!) which I duly took and it was so nice that I ordered one myself. Half way through the dessert Mick decided to show us his ‘Spray the Trifle’ trick, which I copped most of (cheers mate!). After another round of drinks it was back to Dereham, well for most of us it was.

Now to the sad saga of the alarm clock! We sat about in the camping coach aka the Dereham Hilton chatting and the like, (why Gareth and Laura would want to stay in some overpriced swanky hotel instead of the camping coach is beyond me) still it take all sorts to make the world go round as they say. Just before we all turned in for the night, whilst no one was looking, I (Yes it was me!) turned Mickey Doyle’s weird alarm clock’s alarm on. Come the early hours of Sunday Morning we were awoken by some weird gibberish coming from the said alarm clock, and whilst the air literally
turned blue I had to stuff a pillow in my mouth to stop me from laughing out loudly (ouch – my aching ribs!).

Sunday 16th dawns.

We all arose, some quicker then other’s I might add, some were muttering about a feral alarm clock that mysteriously went off during the early hours and what they’d like to do to the person responsible if they ever found out who it was. A certain person was sure it was ‘The Child ‘. The day began with a topping up of water for 56040 then another start up was attempted and guess what – she refused to start yet again. So the call went out ‘send for Garlic’, who arrived and set about the fault finding process yet again.
Having found the fault, a different one this time, this time it was the TDR1 Relay not dropping quickly enough, a little squirt of WD40 and another press of the start up button and she fired up straight away.
Whilst all this was going on Keith Wright was busy in between the Class 31 locomotive and a set of blue/grey coaching stock, coupling up and playing shunter (well done Keith, for a first time you did really well mate, no doubt you’ll be a shunter in no time). I  have also to report to you that there is a very nasty and indeed vicious rumour going round that I do indeed have the cleanest set of overalls of all the working members.
This is simply not true, I do indeed have oil and various other forms of dirt on my overalls.

Hope to see you all at Dereham for yet another crack at 56040 in a fortnight’s time.

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